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From: | Dimitar |
Subject: | Re: [Paparazzi-devel] GPS status NOFIX Problem AR DRONE 2.0 uBlox NEO-6M |
Date: | Thu, 22 Nov 2018 02:21:38 -0700 (MST) |
It is fixed now thanks to the suggestion of Gautier. Thank you Gautier!!! The problem was in the default UART baudrate from 57600in https://github.com/paparazzi/paparazzi/blob/master/conf/boards/ardrone2.makefile#L33 . We changed it to the baudrate configured in our uBlox NEO-6M and everything runs perfect now. -- Sent from: http://lists.paparazziuav.org/paparazzi-devel-f3.html
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